During EMC testing, the robot was loaded with a 3kg load. The test frequency started at 30MHz and continued up to 80MHz. Problems occurred when the force sensor readings at the end effector gradually increased.
robot: ur7e
sw: 5.24
During EMC testing, the robot was loaded with a 3kg load. The test frequency started at 30MHz and continued up to 80MHz. Problems occurred when the force sensor readings at the end effector gradually increased.
robot: ur7e
sw: 5.24